SCCA RUNOFFS H-PRODUCTION RACE REPORT
Man, what a week. We had problems before we even got to the
track, and they kept on coming, but we perservered, and managed
a very respectable result.
We put the car on the dyno Saturday before the race to make sure
the engine was doing what it was supposed to, and
were down on power and couldn't figure out why. During the
couple hours of testing, we also encountered an occasional
mystery no-start while sitting on the rollers. The motor would
crank over, but not start. A few jiggles of wire bundles later,
and we always managed to get it running. Afterwards, we
double-checked everything, it all looked right, so we went
to the track Sunday morning hoping for the best.
Monday practice left me stranded on track after a lap from
the same apparent electical problem. We thought we traced it
down to a connector on the fuel injection harness, but went
out for Tuesday qualifying and encountered the same thing
1/2 lap in. Two sessions wasted. After many false leads,
and tearing through nearly all of the wiring, we traced it
down to a bad Electromotive pickup (a Huffaker, no less)
that would only flake out when it got hot....
I spent a lot of the first couple days looking like this:

We got the problem fixed about an hour before Wednesday
qualifying, and managed to get a full session on the track,
but was tenative, waiting for the car to act up again, and
managed to turn a 1:45, about 16th fastest overall.
Sitting on the grid waiting for Wednesday qualifying to start:

Thursday's session was only 4 laps long after a car farther
back in the pack dumped oil on the track causing a 4 car
mess in the esses, but we found another second of time,
to qualify 1:44, on the final grid in 14th.
I was disappointed, because I figured we had 1:42s
at a minimum in the car based on previous long-course runs
which should have put us top 5.
Alongside all of this, we had been struggling with another
mystery condition which started earlier in the season in
which the engine would run very strong initially, but as
green flag laps click off, the oil temps would rise, and
performance would progressively fall off. In impound
right off the track after the last qualifying session,
we noticed the plugs were really white and it had obviously
been running very lean, although we have deliberately set
the mix relatively rich on the top end.
Marnie and I at impound:

Andy, the very smart guy leaning over the car in the picture
above, surmised a fuel supply problem after long-runs and were
going to verify during Friday morning practice, but 2 laps
in Friday morning, the same car that oiled the track on Wednesday
did it again, cutting our session short, and preventing any
real data collection.
So we gridded for the race qualified 14th, it was a nice, not-to-hot
day, and got ready for the race to begin:

While the starting procedure for this race was
no different than any other, it seemed that time was
compressed, and within just a minute or two of arriving at the grid,
we were entering Turn 1 and preparing to start the race! How the
heck did I get here? We’re about to race!!! I had the best
start of any race I’ve run so far, and picked up 5 or 6 spots on
the first 1 ½ lap, and moved as high as 6th before the mystery power
problem came back, but we did verify via a pressure gauge
that it was indeed a fuel supply problem on the low-pressure side
of our system during the race. Even with dual
low-pressure pumps, our normally 3 lbs of pressure,
dropped between 1/2 - 0 lbs after 5 o r 6 laps and through
the rest of the race! DOH! Mystery solved. The low
pressure pumps were giving out, or possibly a collapse of
the suction lines inside of the cell. We are sure it's not
a vent issue, that was one thing we could verify prior to
the race.
Race Start Video
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Low bandwidth Windows Video:
http://www.midwest-x19.com/videos/Runoffs-Start-Short.wmv
High bandwidth MPEG2
http://www.midwest-x19.com/videos/Runoffs-Start.mpg
I also ran over debris from an on-track crash between two other
cars that occurred behind me on Lap 3 or 4,
and had a RF tire slowly losing air pressure,
so the car was very sloppy at the end. On the way off the
track at the end of the race, #2 cyl exhaust header tube broke
completely off at the head flange! It was hard to keep
track of all of the dodged bullets, and we were very happy
with the 9th-place lead-lap finish.
After the race, Brayden was a big help getting us packed up:

If the car had been running 100%, I'm sure we had a top 5
car, but that’s OK, we'll be ready for next year.
Thanks for all the help, support, emails, and advice
from everyone who helped us through the season!
See you next spring!
-Matt and Marnie Brannon
#22 Fiat X1/9
H-Production